Pristine CTD. Extra cab, short bed, 2wd, SLT. Factory tow/haul package, leather heated seats, heavy insulation package. Rebuilt HX 35/40, Dap injectors, full gauges, PacBrake, Dynamic Transmission vb/servos/accumulator/strut/band/triple disc. Soft tranny lines, 40k trans cooler, lift pump, gooseneck hitch (never used), class 5 tow hitch, tonneau cover, air bags, re- geared to 3.73’s, 3rd Gen brakes with 17" rims Rust free CA truck located in Chico CA, 100 miles north of Sacto. I built this to
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Price: 16000
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Location: Chico CA 95973
Having issues with grimlings appearing into this build, current mileage 227k on original motor. Started all 4 cylinders misfiring on bank 1. Moved plugs, coil packs, injectors, nothing changed. Pulled compression and got 60lbs, was told “you have internal issue”, decided to split block apart and have a look. Only had 1 minor sticky valve on driver head, still had factory hash marks on cylinder walls, no scratching on cam, crank, nothing. So we bore block .20 over, 4340 forged eagle crank, 32t reluctor wheel, 112-500-11 comp cam, h-beam connecting rods, springs, valves, seats, re-serviced heads. After build was told “ pcm “ replace with new vin programmed, didn’t fix, new injectors, didnt fix, setup tune through diablo with specs on build, truck won’t idle run it down road pull data, review through tune setup, guy says “ everything looks good “. Truck has no power falls flat on its face. Now guys say it’s engine harness “ mind you been discontinued since 2015 for 2007 “ no aftermarket is made either. Checked camshaft and crank sensors “ both good “. Did however find driver o2 fault due to no power signal fixed that with piggybacked wire tapping. Anything I might’ve over looked or potentially should or could try ???? All and any help will be appreciated.