Jump to content

Tractorman

Yearly Subscription
  • Joined

  • Last visited

Everything posted by Tractorman

  1. @Thr333_Arr0ws, it may be that nothing is wrong. The following is only my thoughts, but it would seem to me that the ECM easily has the capabilities of operating stock injectors smoothly through all engine rpm's and engine loads, including engine idle. But, when you replace stock injectors with significantly higher horsepower injectors, then I could see that the ECM may struggle to arrive at and maintain a smooth idle. Look at it this way - the engine is going to use the same amount of fuel to idle whether it has stock injectors or high horsepower injectors. The difference would be that with the high horsepower injectors, the ECM would have to cut fuel duration time way back for the engine to idle at the same rpm. To me this could make it difficult for the ECM to precisely meter the exact amount of fuel required to make a smooth transition to idle with high horsepower injectors. I currently run RV275 hp injectors in my truck - that is only a 30 hp bump. While I have no change in the way the engine arrives at idle, I do now have a slight hunting in rpm's at times during clutch engagement. I attribute this to what I just mentioned above and consider it normal. Again, these are only my thoughts - no verification that this is even happening. There could easily be something else going on. - John
  2. I am not going to be of much help here, but can you describe the above in more detail? Is this a rapid change in rpm - such as, 2 or 3 times per second? Or, is this a much slower change? Also, what were the previous injectors - stock, OEM, etc.?. Are the replaced Bosch injectors new, or re-manufactured? Do you know where the VP44 came from and did it come with a new PSG or a used / reconditioned one? I asked these questions because others more knowledgeable than me, will come to your aid shortly and they will probably want to know some of these answers. It sounds like the truck has been well maintained by the previous owner and currently by you. - John
  3. Good to hear that you won with your decision to replace a defective new clutch fan. It's a bummer that you should have to do the job twice, but I am glad to hear the engine is running as it should. - John
  4. Well dang! That shoots that idea. Another area to possibly look at would be to check if there is any dirt buildup on the front side and center area of the radiator. This collection of dirt is caused by crankcase vapors from the OEM location of the engine breather. It is very difficult to gauge how dirty it is. Years ago this occurred on my truck and would cause a minor heating problem on long grades with heavy loads. I spent several months trying to figure out the problem. I even installed a new clutch fan and nothing changed. Once I saw how badly the airflow was restricted (after removing the radiator), I cleaned it thoroughly and re-installed it. On my first test drive, I noticed the engine fan was much quieter under all operating conditions. Previously, the restricted air flow causes so much turbulence around the engine fan that the fan was noisy all of the time. The long period of time needed for the airflow to become restricted occurred so slowly that I never noticed the ever increasing noise of the fan. Not saying this is your problem, just trying to cover all bases. Might worth giving the fan a second chance by driving the truck for awhile after the engine reaches operating temperature. - John
  5. When you are checking out your new clutch fan, are you checking fan operation without driving the truck? If so, it would be normal for the fan to be in full lockup on a cold start, or even a warm start. Normally, driving the truck for several blocks or maybe a mile or so, the fan should unlock. Can you give more detail on how you are checking the fan operation? - John
  6. I have a small mini-excavator - a 2007 Takeuchi TB016 with rubber tracks. I know it is not the same, but it is similar. I bought the machine used with 1550 hours on the hour meter. Still had the OEM tracks. At 2200 hours, because the rubber had many rips and tears, I replaced the tracks with new tracks from Prowler. Those tracks kept coming off - even when I was being very careful with turns. I tried various methods of adjusting them. I thoroughly inspected the undercarriage components and could not find anything wrong. Finally, after 140 hours of operation I removed the tracks and set the new and old tracks side by side for comparison. The OEM tracks were far superior. The photo below shows some of the differences between the OEM tracks and the Prowler tracks. The major difference was that the OEM's steel foundation for the guides was much more robust. The bonding to the rubber was also superior. The OEM tracks are shown in the upper part of the photo. The guides are in far better condition at 2200 operating hours than the Prowler tracks are at 140 hours. Also, the OEM tracks never de-tracked. I re-installed the old tracks and sent my documentation to Prowler. They gave me a full refund. I ran the OEM tracks for another 300 hours while looking for another set of tracks. I finally purchased a set from National. Those tracks are built much more like the OEM tracks. They are working fine (500 hours of operation now). I have de-tracked the Natinal tracks a couple of times, but each time was under severe operating conditions. I think that new tracks are more susceptible for de-tracking just because they have much more traction than the replaced worn tracks. Good traction with aggressive maneuvering can lead to de-tracking. You may want to give a close comparison inspection of your old and new track and evaluate any quality difference. It could be contributing to your problem. - John
  7. I based my response on what you wrote. You made no mention of using the VP44 gear timing mark or using Moparman's article. Now that you have clarified what you did, I think you have adjusted the valves correctly. This would be normal. Once you rotate the engine, some of the valves you adjusted will be approaching a camshaft lobe or just be coming off of a camshaft lobe. You will feel some looseness, but the proper feeler gauge will not fit in the space because the camshaft lobe is not in the right position for full clearance. Always double check your work and you will be fine. - John
  8. No valves are adjusted with engine at BDC. With cylinder #1 at TDC compression stroke adjust: Turn crankshaft one revolution to #6 TDC compression stroke. Adjust the following: - John
  9. Here is what I recall. All trucks from 1994 through 2002 have disc brakes on the front axles. 1994 - 2001 - front disc brakes and rear drum brakes, rear axle anti-lock brakes only (not independent rear wheel anti-lock) 2001.5 - 2002 - front disc brakes and rear disc brakes, four wheel independent anti-lock brakes I think the answer is yes. I believe the RWAL system uses a single sensor at the ring gear location - not a sensor at each rear wheel. It would seem that the ABS controller would not know whether or not the rear brakes are drum or disc. - John
  10. Sound coming from the turn signal cancellation mechanism? It is about the right position of the steering wheel for the noise to occur. - John
  11. Mike (JAG1) and I just arrived at my place about 10 miles northwest of Baker City. I want the thank Mike Nelson for his hospitality and letting us visit for a couple of days. In our defense, we really weren't sleeping in - would you step outside if there was a big guy out there walking around with blue hair and a 9 mm? I don't think so. - John
  12. Don't have my laptop so responding with Tractorman's. Nice to hear from you guys. We had steaks tonight. Yum! Hope you get better Dan. Billy thank you for all your effort on the site Weather is as perfect as ever here now JAG1.
  13. I am assuming the your truck has the single bulb per side OEM headlights that use the 9004 bulb and I am also assuming that your headlights are NOT relayed. If the above statement is true, then your headlight output (in lumens) will be about 50% of bulb rated output because there is no relay. The wiring from the headlights are long in distance and are undersized in diameter, consequently a severe voltage drop occurs at the bulb. Properly installed relays will bring up the voltage at the bulb so that the bulb will reach 100% rated output (in lumens). No matter what halogen bulb system you use, the system must be relayed. If not, there will be no improvement. The 9004 bulb is a low / high beam bulb. The low beam is only 45 watts (for long life). Most low beam bulbs are 55 watts. I switched from single bulb per side to two bulbs per side (Sport Headlights) years ago. Unlike Moparman's experience with Sport Headlights, my experience has been exactly the opposite - good beam pattern and great illumination to the sides and forward (low and high beam). Not nearly as effective as his Morimotos, but far better than the OEM non Sport Headlight. Daniel Stern recommends the following bulbs for the Sport Headlights: The best 9007 bulbs presently on the market are the GE Night Hawk Xenon 9007NHX or the Philips Xtreme Vision 9007XVS2 The best 9004 bulbs presently on the market are the GE Night Hawk Platnium 9004NHP or Philips Xtreme Vision 9004XVS2 I would not have any faith in the quality of the headlights at the website that you linked to because there is only one review and because there are no photos showing the actual beam pattern on the roadway. It is very difficult to buy a good set of headlights on the Internet because there is never any proof that shows how effective the headlights are at doing what they are supposed to do. The Sport Headlights and relays are within your budget. - John
  14. From looking at your photos, the steering shaft can only slide on to a specific position. The first photo shows a space between two sets of splines. The bolt will pass though that space when the steering shaft is slid onto the steering gearbox shaft into the correct position. That is what keeps it connected even if the bolt came loose. Your second photo shows that the steering shaft needs to go farther onto the steering box shaft. There may be a burr on one of the splines. Make sure the splines are clean and add a few drops of oil to help it slide on. Light tapping with a small hammer may help. - John
  15. It is likely to be a poor connection in either the grounding circuit or the supply circuit. In either situation, a poor connection can become worse when another electric load is turned on (the headlights in your case). Definitely check out all ground connections to body, frame, and engine as well as battery cables - both positive and negative. - John
  16. Wonder if the VP44 was replaced yet. - John
  17. Pin #15 and #35 provide power to the transfer pump. One is for run mode and the other is for crank mode - not sure which is which, but it doesn't really matter. The wires are both connected at splice #160. That splice is a potential problem area, but I don't think it is your problem because you are having two problems simultaneously - no fuel pump operation in bump start and a delayed wait-to-start light. It could be that your delayed wait-to-start light is not allowing the ECM to trigger the bump start fuel pump operation. Ditto on what @Great work!says. - John s
  18. Did these two situations resolve themselves? Things must be looking much better now that you have a truck that you can drive again. - John
  19. Before installing the 140 amp fuse, connect an incandescent test tight - one end on the alternator output and the other end on the battery side of the 140 amp fuse holder. If all the diodes in the alternator are okay, the test light should not light because there will be no path to ground. If all is well, install the 140 amp fuse. The 140 amp fuse is not there to protect the alternator - it is there in case a direct short to ground should occur in the alternator or the alternator output wiring. If that fuse was not there, an engine fire could easily start from the heat generated by the overloaded circuit from a seemingly endless supply of energy from two large batteries. - John
  20. Part of your statement here is normal. What is not normal is the blown 140 amp fuse. Need to find out what caused that right away. It is not likely that the alternator caused that fuse to blow. The maximum output of the alternator is about 130 amps. One thing that can and has happened to people is accidental momentary grounding of the alternator output terminal. The 140 amp fuse instantly blows. You have been doing a lot of electrical work on your truck. The 140 amp fuse could have been accidentally shorted to ground right at the PDC location. Because the 140 amp fuse is blown, It is now normal for the alternator output voltage to be higher than normal (22 volts) because the current has no where to go (the 140 amp blown fuse}. The internal regulator (inside the PCM) is sensing that battery voltage is low (which it is) and it is telling the alternator to increase output. That 140 amp fuse is how the current gets from the alternator output to the driver side battery. So, things may not be as bad as they seem. The alternator may be fine. Congratulations on your success with getting the engine running without codes!! - John
  21. A big thank you to @IBMobilefor answering the question about wiring harnesses. - John
  22. I am sorry, but I don't know how to help you acquire the correct part number for a wiring harness. But, I would like to back track just a bit. Are you using a FSM for a '99 year model truck? If so, can you post a photo similar to the one below. The diagram in the photo below is from my 2002 FSM. The wire (BR/WT wire) from Pin 36 goes through Connector 125 (pin 8) and Connector 130 (pin 9) and arrives at pin 86 on the fuel pump relay. The color of the wire stays the same from beginning to end. What does your diagram show? It does sound like you have a wiring harness issue. - John
  23. You would have everything connected so that the electrical system is fully operational. You would find the most accessible test points along the circuit to be tested. In your case the circuit will start at Fuse #3 (20 amp) in the PDC. The next item downstream in the circuit is Joint Connector #2, also in the PDC. One wire leaves Joint Connector #2 and goes to pin 30 of the fuel pump relay. The other wire continues to Splice #161. One wire leaves Splice #161 to an unknown location, the other wire continues to Splice #167. Three wires leave Splice #167, one to an unknown location, and the other two terminate at pin 48 and 50 on the ECM. You would have the ignition switched on and have your voltmeter hooked up to pin 86 on the fuel pump relay to continuously observe the low voltage you have mentioned. With a test light clipped to the negative driver side battery terminal, you would begin probing any accessible place starting at Fuse #3. If the light burns brightly, then you have eliminated that part of the circuit as a problem. If along the way you suddenly find the light burning dimly, then you have located a general area of where the problem is. As you proceed, you are not proving where the problem lies, but you are proving what is working properly - a process of elimination that will lead you to where the problem lies. But, before doing all of that, have you verified that no pins have been pushed back into the wiring connector at the ECM? If everything is good there, then try the following: Disconnect the wiring connector from the ECM. Using a jumper wire protected with a 1 amp fuse, jumper pin #36 (brown wire with a white tracer that leads to pin 86 on the fuel pump relay) in the wiring harness side (not the ECM side). If the fuel pump relay activates and voltage stays high and the test light burns brightly on pin 86 of the fuel pump relay, then you know the wire is good between the ECM and the fuel pump relay. If the voltage remains low and the test light burns dimly, then you know there is a wiring problem between the two location. Please verify the pin numbers that I have given are correct and that my instructions make sense to you before you do any testing. - John
  24. You just gave an excellent example of how using an ohmmeter can lead you astray. One good method for finding poor connections in a 12 volt circuit is to use a test light with an incandescent bulb. The bulb will impose a small load in the circuit and the bulb will glow dimly when there is a voltage drop present. Your "barely touching fuse" would have been much easier to find with the test light approach. I am very interested to see what you find. - John