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I pulled/ dissembled the pressure relief and the bypass valve just to double check I did everything right and I’d heard the Issues with the pressure relief plugging. All looked good. I’ve also got a
Was having over boost issues and when I put air to my wastegate it wouldn’t budge so I pulled the turbo thinking the valve in the turbo was froze. Got it all apart and turbo is nice and free but I noticed that the actuator rod was stretched out pretty good. Does this look normal? Or did the fella crank the waste gate down to get more boost