Pristine CTD. Extra cab, short bed, 2wd, SLT. Factory tow/haul package, leather heated seats, heavy insulation package. Rebuilt HX 35/40, Dap injectors, full gauges, PacBrake, Dynamic Transmission vb/servos/accumulator/strut/band/triple disc. Soft tranny lines, 40k trans cooler, lift pump, gooseneck hitch (never used), class 5 tow hitch, tonneau cover, air bags, re- geared to 3.73’s, 3rd Gen brakes with 17" rims Rust free CA truck located in Chico CA, 100 miles north of Sacto. I built this to
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Price: 16000
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Location: Chico CA 95973
Well to start my story couple days ago I did a 2nd gear launch must of ran to many psi boost and floated a valve on intake number one.. After pulling valve cover lookin for a bent push rod or bent valve found out it just pulled the rocker bolt right out of the head.. We inspected it and found out there were quite a few more threads left just needed a longer bolt so that fixed my valve problem but I notice 2 days later a slight ticking noise sounds like it coming from same area.. Now im led to think maby I got a lifter going out but thought id ask here see what you guys think.. Should of put the 110lb valve springs in long time ago now I am kickin myself.. Any help would be appreciated.. Thanks
Reason i know I over boosted is cause I read from hamilton performance's website they will pop open at 50 psi and I know I over exceeded that.. Never thought this was possible but I underestimated it..
--- Update to the previous post...
After further investigation it turned out to be a slighty bent valve..