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freedomisntfree

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Everything posted by freedomisntfree

  1. I just purchased yhe high idle kit. Wondering where to go for instructions for the install.
  2. I did the sport conversion with OEM units and the harness conversion.... forgot where I got it from Genos or dan sterling.... well I love the output and I'm happy with it ... but I think Id be happier with doing the HID Projector retrofit with Morimito mini H1 bulbs..... I think that is what you are looking for... I should have read previous replies , I guess you already considered the morimotos... my next guess was in fact some light force driving lights to kick on and off on those dark windy roads..
  3. no havent jumped any cars... i made it home ok, I stopped by oreilys and picked up a 140 amp fuse. threw it on and it seems like it shorted as soon as i installed it. made it home on just battery power. tommorow im going to buy another fuse, but before i sacrifice another fuse is there anything i can disconnect before installing it, like maybe the alternator ? like you said maybe the rectifier. alternator is rebuilt by a local shop i wont rule out a bad alternator just yet.
  4. Well I guess I found my problem. Pulled the cap off the alternator fuse and it is blown. That's really odd...
  5. Pcm was a thought crossed my mind. Fuses I gonna check that out in a few .. I post back. All Fuses look good except I cannot get the 140 amp alternator fuse out to check (1position in hood fuse box)
  6. thnx CSM... Batteries are brand new, cables just recently PMed.. transmission wasn't messed with at all.. I'm wondering if the voltage stopped charging is part of a limp mode or something to do with out of whack trans shifting. Also need to know where I can get a new clip for TV ..ASAP Also... when I shut truck off I turned ignition back (engine off) on and volts were back up to 11 ... started the motor and volts stayed at 11, not charging at 14 like normal.
  7. Allright guys. Just as I was getting happy with my truck and trans... I decided to fine tune the TV cable. The last time I messed with the cable I got better results than trans shops. At home I wanted to adjust the tv cable and broke off the clip .. also managed to lose the clip no were to be found. I jerry rigged the cable to get to work. Shifted a little ugly but I expected this. Then my check gauges came on and my voltage dropped to 10 volts. Then down to 0. Made it work fine.. Checked the codes : P1682, 0622, 0743, 1765 ECU P1693 I know they are tranny codes but I need to know if I fried anything. Can i disconnect batteries clear codes, install new clip reset apps and go?? . I have some time before I go home. Thnx for ur help...
  8. I bought me a new filter from AFE. Still going to install the filter minder ... but gave me piece of mind I can rule out the filter for some performance issues I've had lately.
  9. well replaced the alternator. and seems to be alot better. but i need a for sure fix to this, im maxed out on the Fun meter with this issue. also replaced the air filter . Can someone tell me the symptoms of bad governor pressure switch and sensor? i feel like my torque converter locks good sometimes and sometimes it does not lock fully. i know its working i can see rpms not drop fast when i let off the gas sometimes it has good power and sometimes im embarassed to pass i feel like im smoking everyone out and not going far. when the overdrive kicks in i used to feel some good thrust and not as much most of the time . upgraded turbo , 100hp injectors , cold air, edge comp , .... i would think i would have alot more power Burnouts is not my thing neither is smoking people out.... but i tried to do a power brake for sh!ts and giggles and i could barely build any boost. i tried a different day and seems like i build boost ok... it is difficult for me to get my truck to a good shop because of my work schedule . my last resort is AAMCO. but my luck is they have it for a day and tell me truck is fine.. i would pay some good money to have someone here local help me out. i have dumped lots of money in this thing lately not to have power on demand. im doing another long roadtrip pretty soon and need to have some peace of mind everything is running the way supposed to . she hasnt let me down yet... but .... last thing, the only thing i remember messing with prior to is the tv cable, to change my 1st to 2nd shift point from annoying 2200rpms to 1700 rpm. thnx in advance fellas
  10. Sorry for late response... my switch is still in. And seemed to work only sometimes. Yesterday I unplugged the alternator wire and drive and now everything Eems to work sweeeeet.... for the time I drove with it disconnected. I'm on my way to get another alternator. Tired of dealing with this. I going to have the alternator shop test it and test their own as well
  11. I agree on the filter minder.. would be a good addition. Although I can say I had one on a powerstroke a while back and I never seen the device show any type of restriction maybe I just kept a good filter the whole time ... I'm going to dish out for another filter just to rule it out and have oiece of mind. ... thanks guys
  12. Ok guys I been known to ask some Jerry Seinfeld questions ..... but I just need to know for sure... My filter has been on the truck atleast 60k miles. I've washed it the proper way... I don't normally put air pressure to it... but I decided to just to feel how much air I would feel passing through the filter.... I pushed some air from the inside out and could hardly feel any air going thru the other side ... I been having trouble getting above 25lbs of boost lately ... and I want to rule out the air filter .. .. any input on this is greatly appreciated
  13. Going to go thru all the grounds when I get home this weekend. ... definitely gonna check out the alternator.... any suggestions on where to get an alternator that has been tested already for noise interference? ?
  14. well guys..... i havent been able to diagnose the problem with my TC issues.. i took my truck out after letting it sit for most of the week and check engine light was gone.. Truck drove like normal. no issues. Im sure check engine will come back. Just wondering what the problem could be. I did notice every now and then shifting a little rougher than usual. Speed sensor maybe??
  15. Thnx for responses gentlemen. That's alot of info I need to look over... Moparman CSM .... i won't know till I get back to the house. Gonna cut my wkend short I don't want to stall out in traffic tomorrow. .. I'll post back. Thnx
  16. Well went to San Diego 100 mi drive. Started my truck noticed my RPM gauge not working. Shut off the engine .. when I restarted it came up with check engine light and some codes I'm assuming have to do with TC switch. codes my dash came up with... Pcm 0622 0743 1765 1694 1693 ECM 1690 1693 .... i need to know if my truck gonna stall on me. Thnx.
  17. going to try and find me a digital voltmeter. im assuming i check the voltage key on engine running or just key on .. ? what is the voltage im looking for
  18. glad u guys helped out with this..... i been messing with it for a few hours now that Las vegas goers are gone. I have to say i like it. I can confirm my coverter is working ok. Seems like the trans downshifts on its own more than it wants to stall if i leave TC locked. I was cruising on a main street 40mph at 900 rpm... i like that manual trans feel. Ok, now that i know the TC locks up with the switch, what next? is my problem the PCM . another thing.... Although i like the switch, and i would like to keep it.. i want the best of both worlds, or back to stock mode. i read somewhere about a 3 way switch.... stock, locked ,unlocked... ???? still need to find the problem .... thnx
  19. the part im still confused is do i start of with the switch off or in the ON position.... edit.... ok i think i understand after reading a few more times ... i will post back in few hours ... thnx guys
  20. gonna head out and find me a piece of road after rush hour.... thanks a lot for the info
  21. just installed my lockup switch. im confused on how to properly use it. my first trip around the block it wanted to stall at a stop, so i switched it to the ON position (UP), and i was back to normal. took it out on the highway and yeah i guess its working, its hard to find a good spot to really get on it or play around because so much traffic here. After playing around with it, and coming to a stop it wouldnt stall in any position on or off anymore. . so this has me really confused., truck should stall if it engaged right? when do i engage it and disengage.. .... I need a Barney style explanation on this switch. my main objective here is to understand how this TC switch works so i can find my issue.. thnx for any help
  22. roger that ... pretty much the answer i was looking for ... thnx for the input.. gonna try and install that switch this wkend and hope for the best.
  23. no codes no check engine... trans is a DDT . i dont have any details on it but its been in there for atleast 40k miles
  24. well... i just dumped $1500 in front suspension..... put in 100hp injectors ran fine lots of power. running out of funds to dump in this truck. Now that i had her running the way i want, i lost torque converter lockup. Im not the greatest when it comes to transmission department. but i dont feel the kick any more after 40 mph. and at highway speeds i have very little power on my 5x5 setting . i thought maybe my air filter (AFE pro dry) could be restricting becasue i noticed it has a few kinks in it like it imploded. washed it out and dont feel any difference. I have had locking/unlocking issues before and was advised by moparman to remove the noise filter...... well i had planned to but havent done that yet. before i go installing a TC lockup switch i would like to know what im up against. I have read many threads and not gathered what im looking for. Does this mean my trans is shot? it shifts through the gears fine i can get up to 80mph on level ground... rpms seem a little lower than usual. trans temps seem to get hotter quicker 210 last time around traffic on a hot day (90deg) thanks fellas fuel pressure is good 14psi filters are good timbo apps new batteries new alternator is atleast 2 - 3yrs old