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Has the clutch engagement position of the clutch pedal changed when the problem started occurring? If it has not I would suspect that there is not a problem with the master / slave cylinder operation
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2 months later and the tranny is shifting better. I was sure there was some air trapped in the master the way I installed it. Just like the first time it has gotten better with time. So there seems to
Been having some trouble shifting gears lately. Leave out in the mornings and shifts fair to good. Get some heat in every thing and l have mash the pedal into the floor pretty good to shift. I replaced the oe master cylinder back 2008 but it was leaking by and creeping on me and then failed all together. That one was fun since l couldn't find any way to bleed it and didn't know any better. Did the best I could but still had some air in it. It took about 3 weeks of driving and a lot clutch pumping but finally settled out and has been working fine until a 3 or 4 months ago when this started.
I had a replacement here and today would be good to swap it in. So googled a little bit to see if any one had better way. Low and behold the first video l look at is @Mopar1973Man swapping his out long ago. He swapped both master and slave and removed the whole system and bled by using the slave. I did not want to go that far. So l was able to get the MC out far enough to keep the line to the slave about level and near as l can tell lost no fluid from it. I tried put fluid the new one on the resevoir side and it would not take any. I was succesful in getting into the output side but slowly. Kept adding a little at a time until bubbles quit coming out. I was able to keep the MC inverted and connect it to the line with hopefully no air in the line. It is working about the same as before.
On the funnier side when l removed the upper bolt and was pulling the socket and extensions l lost the nut. I spent 15 minutes sticking mt hands in any space they would fit looking for said nut. Nothing. While installing the new MC i had shine light in there and low and behold it was stuck between to pieces of sheet metal above the bolt. First time l ever lost a piece of hardware the defied gravity.
Anyway figured l would go for a test spin. Looked at the cluster and the CEL is on. Check the code, p0237. Lost another MAP sensor. Damn. This is under warranty though. Thats 3 in the last 4 years.
I am not pulling tranny till it to goes to shop for new synchros and such. Hope tomsend it to Super Stick in Texas for a refresh. Dont know anyone around who knows the 5600. No odd noise from anywhere in the tranny just getting harder to shift after warms up. Could be the pilot bearing I guess. Any thoughts are welcome.
Edited by dripley