2nd Generation Dodge 24 Valve Powertrain
This is a discussion forum of the 1998.5 to 2002 2nd Generation Dodge Ram Trucks with 5.9L Cummins 24 Valve Turbo Diesel power train and drive line system. This includes all sub-system including wiring, fuel, oil, exhaust, air, transmission, computers and sensors.
6,288 topics in this forum
-
2000 PPUMP 4x4 Pulled batteries to put on charger last nite as well as radio to install a new one.Both batteries 12.4V ....Truck wont crank at all - not even try. Starter fuses and relays look fine/ Switched them around with some others in PDC and no difference. Ideas on what to troubleshoot ? Had same issue when I came back from holidays. Pulled starter and it checked out ok and switched fuse and seemed to fix but fuse seems ok. thx
-
-
- 15 replies
- 2.4k views
-
-
I recently bought an upgraded vp44 from Blue chip diesel ($1600) because my original died. After installing the first pump the truck started right up and ran great for about 10 minutes, then I got a code saying injection pump timing failure. I talked to Chip and he sent me another right away. This second pump has been great for about a week. Now for some reason around 1,000 to 1,200 rpm when I mash the go petal it loses power, makes a horrible lugging sound then picks up and runs fine. I am also having trouble starting. Warm or cold it doesn't like to start on the first crank and sometimes it won't start on the the second. This doesn't happen every time I go to start it t…
-
-
- 35 replies
- 4.9k views
-
-
So just a general question I have an hx35 want a good filter was wondering if putting a cold air filter directly on the turbo would be good or bad seen a few around need some opinions thanks
-
-
- 11 replies
- 1.8k views
-
-
Just wondering if anyone has used these gauges? I just received fuel and egt gauges. They seem like nice gauges, they have a high and low warning light and they are not overly expensive.
-
-
- 14 replies
- 2.5k views
-
-
Well I got my ISSPRO 3 gauge pack in and I got it installed. I ran into some problems but gave Michael a call and he helped me sort some things out that I wasn't paying attention to. I ran out of time at my shop and daylight but went on a test drive at the airport and Airdog 150 is holding rock solid 18psi at idle and 15.5psi WOT in 4th gear pull. I am also pulling 21psi peak boost on my stock truck and I think that is pretty good. All in all I am really happy with the Airdog and the ISSPRO gauges. I will try to finish up the EGT and lights and maybe a video if any one is interested tomorrow. Thanks again Mike!
-
-
- 20 replies
- 4.2k views
-
-
-
I bought this truck about 5-6 weeks ago so just now finding all the bad habits. So only one time a day (mornings) the oil pressure gauge wont come up, check gauges light comes on. So I turn it off start it back up and its fine the rest of the day. At first I thought trash in the sender but its every day. Oh and its the 5.7 Hemi
-
-
- 3 replies
- 1.7k views
-
-
The other day I smelled a strong smell of diesel fuel and I pulled the truck over. When I looked underneath the truck there were over a dozen driplets dripping off the driver's side frame rail. The frame rail was completely wet. Diesel was also dripping off the transfer case skid plate. I recently installed a Fuel Boss fuel system on my truck. My first thought was maybe one of the new rubber hoses chafed on something, even though I was extremely careful on installation. I determined the leak was between the tank and the frame rail. After several drips of diesel fuel on my face, trying to peek in the gap between the frame and the tank. Since I was on a road trip an…
-
- 6 replies
- 4.8k views
-
-
Fellas, is it going to screw anything up computer wise by taking my both batteries out for a few months? I lay my truck up would like to take the batteries out and trickle charge them all winter. I store it to far away from a power source to leave them in with a trickle charger on them while in the truck
-
- 13 replies
- 1.9k views
-
-
Hey folks, This is my first winter with my Pacbrake. It had run flawlessly until ambient temps got down to around 10 degrees. Then it stopped working on my way home one night. The next morn. after I warmed the truck up for an extended period, it started working again. This cycle went on for a couple of days, then my 30 amp compressor fuse blew. I replaced the 30amp with a 20 amp. ambient temps are now around 32 and she's back to working reliably. My compressor is located by the passenger side battery as directed in the pacbrake instructions. I routed the air intake filter to the firewall behind my Bhaf. I have not yet remote mounted the actuator piston vent that pacb…
-
- 6 replies
- 1.4k views
-
-
Hi Guys, Just came across another Bosch authorized VP44 pump rebuilder - here is the link. http://www3.jasperengines.com/blog/2011/12/02/jasper-remanufactures-vp44-diesel-injection-pumps/ The link shows the actual "diaphragm" that is installed in these pump that fails regularly - so Jasper claim. Anyway, I just thought that this link might be of some interest. Thanks
-
- 3 replies
- 1.9k views
-
-
-
Today I was heading home from work and when I turn hard left or right the trans acts like it is not in gear, if you let off the throttle and get back on it, it kicks back in. What would cause this? I just put a new rear speed sensor and output sensor on the tail of the trans. i do have a new neutral safety switch to install yet.
-
-
- 5 replies
- 1.4k views
-
-
Hello all! Ongoing issue with APPS. Truck developed heavy miss between 12 and 1600rpm wether truck is cold or at operating temp. No codes in computer, no CEL. Tested voltage of factory APPS (after trying resetting it) .54-.79, dropped to .51-.59, jumped to 1.02-1.73, dropped 1.51-1.57, jumped 2-2.7 etc. eratic voltage all the way to WOT at 3.81. ok, bad APPS. New timbo APPS installed per instruction, reset everything, started and miss is gone. smooth voltage .68-3.79. drove 1.5 miles and parked for three days. started back up, truck missed and loaped for ten seconds at idle (never happened before). idle cleared up, but same miss is back between 12 and 1600rpm. No CEL…
-
-
- 14 replies
- 4.4k views
-
-
In 9/2012 my tail pipe rusted out so I had a new tailpipe put on. Now the muffler has rusted out in the front where the resonator connects. The the muffler going in is 4" and coming out is 3"My truck is completely stock and I've only put 4000 miles on it in since 10/2011 So my questions are.What if any advantage is their to delete the muffler and just go 4" from the resonator back.What if any advantage is their to delete the muffler and neck down from 4" at the resonator to 3" that is the stock size of the tailpipe.The muffler shop wants around $250 for the new muffler. Money isn't really the issue here. It's just the fact that I really don't drive the truck that much.
-
- 6 replies
- 2.1k views
-
-
Mike, would you happen to have the lube properties of 50/50 fuel, which was 'cut' with a benzene xylene 'anti cloud/jel' product?
-
- 2 replies
- 1.6k views
-
-
don't know if this is the right place to ask this , how hard is it to install a elec fuel press gauge ? looks like i have to put it in the bottom of the fuel filter canister ? also how hard is it to do a raptor or air dog with changing all the fittings and droping the tank ? im not that bad with mechanics , i did the a/c evap in the truck and the a/c compresor
-
- 6 replies
- 1.5k views
-
-
-
Was looking through Fuel pump options and came across this place. industrialinjection.com They rebuild fuel injection pumps for diesel engines and tout their abilities, as do all companies, however, may be something to it... http://www.industrialinjection.com/shop/category/pumps/dodge-injection-pumps/ Curious if anyone knows of these guys or not, interested about experiences.
-
-
- 21 replies
- 3.7k views
-
-
it was 'CCd' on the overhead display for awhile. I toggled through the different displays, and finally just turned it off. When I restarted the truck awhile later, all seemed ok.on another matter, truck refused to start 5 days ago, plugged in overnight, and battery charger to boot. I gave up quickly just because I had 3 tractors 'dead' from crap fuel that needed attention first! This morning It got up to 25*, so I tried it! It stumbled to life and within 3 seconds it suddenly was running on all 6 cylinders. Perfectly. Other than 30-40* warmer than last Friday, I didn't do anything different: same fuel…
-
-
- 5 replies
- 1.4k views
-
-
Bought the thermostat and a gallon if coolant. What's next?
-
- 16 replies
- 5.6k views
-
-
Well it has come time to rebuild my transmission. Ive recently replaced the governor solenoid and sensor, adjusted bands and replaced filter and fluids. Well now it is not down shifting. The forward band is worn beyond use, and I'm sure that with the shifting issues I've experienced over the last two year that the rest of the internal works are worn just as bad. Ive adjusted bands, changed fluid and filter, adjuster TV cable, replaced solenoid and sensor, and still no improvement. So it is just worn out, closing in on 200,000 miles with a stock tranny, I can't complain. :lol:So I'm doing the Sun Coast M3GA 3 Alto Transmission Kit, Sun COast Triple Disc Torque Converter, …
-
-
- 10 replies
- 2.4k views
-
-
up here in ND now and we just got super cold weather and now I got number 1 in its been -15 for the past 3 days now and I have a problems of jelling up. I know the tank isn't Jelling up anymore it just when I go driving around I start to jell up and I think it comes from where the airdog is mounted and not getting any heat. I was wondering if anyone else has had this problem with Filters to cold.
-
-
- 40 replies
- 8.9k views
-