Pristine CTD. Extra cab, short bed, 2wd, SLT. Factory tow/haul package, leather heated seats, heavy insulation package. Rebuilt HX 35/40, Dap injectors, full gauges, PacBrake, Dynamic Transmission vb/servos/accumulator/strut/band/triple disc. Soft tranny lines, 40k trans cooler, lift pump, gooseneck hitch (never used), class 5 tow hitch, tonneau cover, air bags, re- geared to 3.73’s, 3rd Gen brakes with 17" rims Rust free CA truck located in Chico CA, 100 miles north of Sacto. I built this to
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Price: 16000
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Location: Chico CA 95973
I just got the head back from the shop. Measure 0.007 of warp, no cracks, 6 bad valve guides (all exhaust), and the #6 exhaust valve was bent near the keepers.
The bad, no smoking guns as to why the gasket failed. Any ideas? Maybe I didn't get the head torqued correctly? It lasted about 10,000 miles before it failed. It did not mix with oil or get into the cylinders.
Unfortunately, I did not grab a picture of the gasket I pulled off, however, I have a doodle of the new gasket as to where it failed.
The red is where the gasket failed, the blue is the path of the coolant. It failed near #2 and #5 and was starting to fail on #3&4.