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Yup. It finally happened to me. Dropped from 5th to 4th rolled up my power tried to shift to 5th again... NOPE so I'm stuck in 4th limped into Hoots Cafe in Whitebird, ID. Im glad my sockets with me. Quickly pulled the cup holder up. The the boots. Then the shift tower. Everything was good just jumped out of the gate. Push the center fork back to neutral. Reassembled. Took 20 minutes with basic tools. Now in Grangeville ID getting breakfast.

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  • Dieselfuture
    Dieselfuture

    Wow, just think if someone had no idea what to do next, probably cost them few thousand bucks to deal with that. Good thing you had some tools with you. So is this something that may have been overloo

  • Mopar1973Man
    Mopar1973Man

    Like I said the front two tower bolt were not tight so when I pulled down to 4th I pull the shift rod right out of the gate. If the tower was tight it might not have happened. Being I normally just st

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12 minutes ago, Mopar1973Man said:

I'm talking about PenzOil Syncromesh. It does not meet the synthetic spec. 

Sorry about that, thought it was a broad statement on all synchromesh. At the same time the guy I know that has a transmission shop for last 40 years told me if they are unsure what to put in they use pennzoil synchromesh and never had a failure due to that oil. :shrug:

Penzoil is all i have used for the 320k or so miles on this trans. The first 52k were most likely the Mopar since I bought it used