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Mopar1973Man

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Everything posted by Mopar1973Man

  1. Yes it could... Even though the block heat might make 90 to 100*F temp b ut blowing outside air can upll that down. Then when you start the activation of the high idle 6 CYL just needs. Coolant below 140*F IAT below +32*F with grid heater running. 3 CYL... Coolant below 140*F IAT below +15*F with grid heaters running.
  2. IAT temp has to be below 32°F with the grid heaters running. So it's got to be colder than 32°F to actually trigger 6CYL high idle.
  3. Now your back to replacing the multifunction switch...
  4. Still the fact the issue never changed between new or old part. Same results. If it wasn't right I should got some change like nothing or all working.
  5. Yes. I've got one left let me correct the store... POOF! (Magic dust every where). One sitting on my desk.
  6. Be aware without a tuner the stock ECM is fairly retarded in timing so it does emit more smoke because of this. Then the ECM doesn't know there is a change from Stock to +50 or +75 so the fuel map will be too fat and tends to smoke on launching. Then EGT's will be higher being the retard state of timing. Bigger the injectors the more timing you need to make it efficient. Like I'm running close to 21* @ 2k RPM's. Stock is like 14* @ 2k RPM's. Matter of fact... I've been talking to @dieselautopower (Jacob Kid) and there might be a spot for me as a "tuner tech" for Quadzilla. Still working out how we are going to do this. I've had another vendor ask if I would build tunes for their customers as well. This is still in the "works" right now but soon...
  7. 6 CYL Mode requires the coolant <140*F and the IAT <32*F with grid heaters actively heating. Typically close to 25*F outside. 3 CYL Mode requires the coolant <140*F and the IAT <15*F with grid heaters actively heating. Typically close to +5*F outside. Quadzilla anything below your set "Warm up" temp will lock the tuner to level 0. Then waits the delay and then starts 1,200 High idle.
  8. I would say it depends on the tuner that is going to control the timing and fuel aspect of the injectors. Like my old problem was my Edge Comp only basically stacked on +2 or +3 degrees of timing on top of the stock table for the most part. This is part of the fight of why Economy on the Edge sucked. You had to keep your engine load down by slowing down to get the good numbers. The fuel table was more or less treated the same way. Edge Comp had super poor control of fuel and smoke even with +50HP injectors. Consider your tuner. Like today I run just about smokeless on my normal level 2 (stock fuel and added timing) or level 3 (CanBus Fuel and timing). I can handle +150 HP injectors no problem towing even is awesome being close to 18,000 pounds and over 60 feet long and no EGT's issues. ILLEGAL ACTIVITIES Yesterday I knew that @Wet Vette went to the doctor appointment in McCall. She called and ask if I wanted something before she came home from McCall. I was finishing up down at the other shop (Russ). I packed up myself and ran back up canyon towards New Meadows, Found a nice pull out facing toward home and just waited. Eileen found me and pulled over I told her I wanted to "play" on the way home. Needless to say she snagged lead leaving the pull out and as we broke out of the canyon on the first straight I wound the Cummins up passing her at +90 MPH easy and took the lead from her in her Hyundai Elantra. Then we proceeded as a team to run over 80+ in 65 MPH down the windy canyon towards home. Ran like this for over 7 miles and never missed a beat. Pulling corners marked for 65 MPH at 80+ MPH the whole way back. Fresh track bar and Blue Top Steering it was running like a slot car. Eileen stayed tuck in at my rear bumper. Both of use had to hit the 100 mark at least once. Even with 30 inch tires ratio (3.69:1) is awesome pulls super strong on the top end. Brought me back to my old street racing dayz once again. I felt like a teenager once again. Needless to say it was a head rush!!! Both got home smiling...
  9. No, he could not even attempt to handle a redneck gal...
  10. (Gotta say thanks for the other info) Basically the fuel get above 150*F creates asphaltenes that make a material that is like a tar sized at about 2 microns. I'm thankful I use quality filter on the AirDog and the stock filter can. I'm double filtering. Then since I don't return and pump out of the sender basket my fuel stay much cooler. Since I kept the stock filter can I still have my WIF light functional, the electric fuel heater is still working, absorbing heat from the manifold, etc. Being my fuel temp hovers with IAT temperature with (+/- 5*F). My filters go upwards of 60,000 miles. Back when the truck was stock everything. I had problems with asphaltenes building in the fuel filter. Now with the AirDog 150 flowe enough to keep the over flow valve open and double filtering my VP44 stays cooler than most and double filter protect the internal parts of the pump from wear. Then if you add 2 cycle oil on top you now just gave the VP44 the best chance of living a super long life.
  11. Other way is to smack the pin in the Torx screw and break it off with a small hammer and punch. Super easy.
  12. That's one thing Morimoto HID's D2S Lens, does not have is pair of hot spots. The light is evenly cast over a surface. Then it cast farther and higher that most all other solutions. Like @dripley photos the two hotspots won't be there. Now expand the light cast along the edge of the road out another 50 feet out both directions.
  13. I think it's a group 27 IIRC. 31 might just squeeze in but typically the tray is quite big enough. Stock requirements is 750 CCA. Like the Walmart batteries I got are 810 CCA. More than enough to handle subzero starts for 10 plus years.
  14. That would not be much of a upgrade looking at the exhaust housing its a 9cm2 or appears to be. A true HX35W would be 54mm in compressor wheel, 60mm on the exhaust turbine, then the housing is 12cm2. My HX35/40 Hybrid is 60mm compressor, then 60mm turbine wheel, then the housing is 12cm2.
  15. Yes that is good. I'm set to the same time delay. Quadzilla yes. Cummins ECM No. The ECM software will cancel if you touch the brakes. Usually as the time runs out mine snaps instantly to 1000 to1200 RPM. On cold morning it might hang a bit low hanging at 1000 to 1100 RPM it not set by RPM on the Quadzilla but rough fuel amount. Yeah. That normal as the grid heater fires it drawing roughly 95 Amp and with cold start and batteries needing charged the alternator is most likely maxed out hence why when the grid hit the volt needle falls a bit.
  16. Hence why my filter go 60,000 miles with any issues. I rarely ever see fuel temp even near 140*F. @LorenS thanks for posting that temp so now we know 150*F is the point asphaltene start to create. Again I'm not drawing from the fuel basket but from the tank.
  17. Yes that is the AirDog water separator and prefilter. It does work pretty good at both typically there is most of the water caught here rarley do I ever see water in my stock filter can. I've used Donaldson, AirDog and Fleetgaurd filter all look to be about the same design.
  18. Could be as short as 15k miles if your getting farm fuel from tank or if you going to the fuel station maybe 60k miles. All depends on your source of fuel and how clean said fuel is before you pump in your tank. AirDog 150 pre-filter and water separator. Now the filter never really ever fills up or plugs on these. When you change the main filter I will shake this on up a bit and the dump it out. Just screw it back on. I only check for rust damage and keep reusing the pre-filter. Now as for that little in-line filter you have to throw it out after a cycle you can't wash then out very difficult...
  19. I just got my 2005 Dodge Ram customers steering box back on Monday. Now Wednesday I'll go to install this box. I'll try and remember pictures. I've got a Blue Top (Quick Ratio) in my truck and its Tight! Like Race car Tight! I did readjust the sector adjustment of the output shaft to get the last bit a of slack out.
  20. Can you post a picture of this turbo so we all can see what your working with and then could you shot a clear picture of any tag or model numbers so we can look pu specs if possible?
  21. It's OK but getting up there. I would suggest doing the W-T ground wire mod. I'm still down around 10mV AC (0.010 ACV). It will help a bunch.
  22. No, as long as you buying the stock OEM relay made for the truck. They are design to do this job for years. Personally I fire up and get moving as soon as possible. There is nothing worse that starting a truck leaving to idle at 800 RPM having the grid heater clicking on and off to heat the manifold drawing more power than the alternator can produce at 800 RPM. Like I said I typically unhook the grid heater in April and leave it unhooked till October. All this time the relays can do what they want but no power present. But yes starting and leaving it idle 800 RPMs is the absolutely worst thing you can do to the alternator on a cold start. If you had either my high idle kit or the Quadzilla where you can high idle now at 1,200 RPM now the alternator can handle the loads between being it like being driven 20 to 25 MPH and the alternator can cool the diodes because of extra fan speed in the alternator. Back to the batteries if they are weak every time the grid heaters heat then the load majority on the alternator since weak battery normally won't carry much of any loads. Again now you end up with a hot alternator attempting to burn up the diodes.
  23. Comes from the ECM. You see the ground is supplied by the body ground and the ECM controls the +12V to the relays.
  24. No. Because I was stuck in Ontario at night without a alternator so I cored it out and had it test it failed completely as for what I have no idea since I wan in Ontario and no time to pull it a part in a parking lot with limited tools and knowing my PCM was fried at that point it was done. Still in all... If you short the green wire to ground you get a runaway alternator that is overcharging. No damage to the PCM will occur. Now short the blue wire to ground and PCM will fry. Heat is a sign of high electrical loads. First place to start. Also sign the batteries and/or cables are not up to the task.Weak batteries or shorted cell battery will still cause the alternator to get hot. Just like my landlord at my second shop he was using his winch for long periods with bad batteries and blew the alternator fuse. Again the alternator is not suppose to hold all the heavy electrical loads, that is the batteries job but if the batteries are not up to the task then its handed off to the alternator and in turn shows up as heat. As the load continues the alternator burns up brushes and/or didoes. So far I've never seen winding burn... Here again that glowing bolt is a sign of poor connection again points back to what I said of poor cabling or connections. You could of seen this using the voltage drop test and would of been high volt number there. I'm sure higher than 0.2 volt drop. Remember this same test can be uses on "ALL WIRING" of any vehicle right down to small engines like motorcycles and all the way to semi-trucks. It can be used on any circuit to measure voltage loss as the circuit is running. Optimally you want ZERO voltage drop. Less is better but in the article it calls 0.2 volt drop a fail for starting cables. Now a example of this in action. I had a 1982 Honda Sabre 750cc V4 motorcycle the cluster was semi-digital. When I was riding at night and using my head light and fog lamp (up graded to 100w) both the cluster would spit out weird things at times. This point out I've overloaded the stock ground with the added wattage of the fog lamp. Come to find out the master ground for that motorcycle was under the fuel tank and was only a 16 gauge wire. Only ONE ground. After measuring I was getting 0.3 volt drop on the ground circuit. I added one extra ground up by the headlight and fog light to aid in this voltage drop afterwards drop 5 to 6 mV DC. As you see... That was a change I made to improve light which came at the cost of overloading the master ground after allowing for a extra ground problem was gone. Now using this information this is why on my truck I went the other direction and REDUCED the electrical loads and now gaining ground and not having the alternator issues like I did. I've double and triple check this on at least THREE different trucks. I know the W-T ground mod does work! As for the parallel ground does not gain anything in the THREE othere truck I've try it on. People tend to forget I'm not just working on my truck and testing but working with many owner and trucks and seeing if there is any change. As for the parallel ground it OPTIONAL in my mind and going to do anything for ground performance. Being all them resulted with and without parallel ground in the 2 to 8mV drop that doesn't change on good master ground cables. I can see it for W-T when hes got linear, ham radio and high current draw with a need for absolutely CLEAN POWER. Any noise is brought back to the radio as frequency noise in the back ground. Hence why he's done noise mods to his AirDog pump to cut out the RF transmission from sparks created at the armature of the pump.
  25. Common though is to replace the multi-function switch first. Being the wipers are typically a different circuit but the contact might of failed and touching off the wipers for the left turn side. Another common issues is usually function quit completely is constant use of the tilt function of the column typically breaks the wires to the multi function switch or the ignition switch. Wipers Turn signals.