2nd Generation Dodge 24 Valve Powertrain
This is a discussion forum of the 1998.5 to 2002 2nd Generation Dodge Ram Trucks with 5.9L Cummins 24 Valve Turbo Diesel power train and drive line system. This includes all sub-system including wiring, fuel, oil, exhaust, air, transmission, computers and sensors.
6,275 topics in this forum
-
Has any one converted there front ends to the old style lockouts so the front end don't turn all the time and if so were do you get the kit? --- Update to the previous post... here is a link i found http://www.emsoffroad.com/store/index.php?main_page=product_info&cPath=128_131_134&products_id=330
-
- 5 replies
- 1.6k views
-
-
Ok so to start this started in the winter. When i first fire my truck up my voltage bounces from 13 to are 6 till the engine warms up then it would start charging like normal after 5 to 10 mins. No big deal i started it let it run before i go to work. Now that it is warming up. I start it and if i touch the pedal and bring in even little bit above ideal the voltage drops to around 6 and stay there. Until i let the rpms drop. Then it will bounce around then most times come back to normal. Long story short put a alternator two weeks ago and a computer on the fire wall. I have had it to the stealership twice and they always come up with something retarded that they think it …
-
- 9 replies
- 1.6k views
-
-
I have an '01 Dodge diesel 3/4 ton that I rebuilt the engine on and it started right up after bleeding the fuel lines it started right up and ran fine. One of the batteries was dead and I replaced it tonight and went to start it up it just turned over like it wasn't getting any fuel. The overhead display read "CCD" and the engine light was on. The scanner pulled P0122 and P1698 codes. P0122 looks like throttle positon sensor and I can't find the P1698. Could replacing a battery killed the TPS sensor or was it just coincidental? I'd appreciate any assistance or insight anyone has on this.
-
-
- 6 replies
- 1.6k views
-
-
Im corn fussed ?? replaced the injector pump and now i have an issue with excessive oil blowby ,its seems i need to be going better then 55 for this to happen ? any suggestions were i should b investigating first, thanks .
-
-
- 9 replies
- 1.6k views
-
-
I sent the controller off to have it checked to see if there are any problems, and I got a call today that said the entire cable was corroded and corrosion was inside on the board. I think oh crap what is that going to cost? They tell me for the 99.00 fee for check up they will send a new updated controller. I guess we shall see.
-
- 6 replies
- 1.6k views
-
-
Ok,I consider myself somewhat knowlegable on my engine. Some history first,I drove to Springfield IL to pick up a trailer,delivered to KS,noticed that vaccum pump to front case was leaking,went to my local cummings dealer for gasket(not a big deal,done several times before). Left to pick-up a trailer in Des Moines going to SD,truck purred like a kitten for 130 miles at 72 mph,loaded trailer and headed out,30 miles later felt a miss,loss of power,pulled in to a fuel stop a mile down the road,lifted hood to see oil all over the place(never lost good oil pressure(40-45 psi)20 psi at idle,shut truck down.Found that oil was leaking from push rod cover(this is where I get confu…
-
- 7 replies
- 1.6k views
-
-
Ok gang I got vp 44 installed and now shifting is grate, no rpm drop, now shifts nice and smooth. But, there is still a problem with shurging when slowing down or push clutch in it surges about 4 times then smooths out. I put new timbomb apps and the lowest we could get numbers down to are .671 is this to high, in other words is apps sending a message to ecm searching for idle mode? Tim said .671 would be ok, I am wondering if there may be a problem here. Oh yea, eng. died several times with old vp and never thru a code. I got to ask what's up with that?
-
- 3 replies
- 1.6k views
-
-
98 1/2 2500 2wd 5.9L auto. Normally, turning ignition switch to run position and waiting for the WTS to go out, starts a prime cycle on the lift pump that I can hear, lasts a few seconds and turning key to start position starts this truck immediately, I mean in like half a crank. Lately, I have had intermittent issues where the WTS lights normally and goes out, but I never hear any lift pump prime and the truck has an extended crank time of 5-10 secs before it starts. Once it starts, it runs great, fuel pressure great. But the problem is intermittent. It will work normally for a week or so, and then exhibit this problem..... I know Mike said in previous posts that a miss…
-
-
- 19 replies
- 1.6k views
-
-
Good day everyone, Have a few questions regarding rear main seal replacement. 1. Do I need the $200 tool to install the seal? 2. What kitsch have you guys used to not need the tool? I have to replace my seal, but don't want to have to dish out extra money for a tool I may use 1-2 times. Thanks, Tim
-
- 7 replies
- 1.6k views
-
-
I dont know but I may have found something. I was pulling starter to clean ground wire on block when I noticed the small ground wire on starter was lose, so I went to tighten it and the groment was lose also so I said I will take it apart and tighten it, they usually have two nuts one on the inside. Well not this one, the only thing that keeps it from turning when you tighten it is the copper wires inside housing. So when I put new starter on I my have broke the wires inside starter or made a bad conection. So here is the million dollar question if the ground wires inside starter are loose or making bad conection will it cause the eng. to die for a split second then cont…
-
- 2 replies
- 1.6k views
-
-
Hey guess I'm finishing up my p 24v ! I was wondering what a good timing setting would be on s daily! 12mm pump, 63/68 over an 80, 6x16 injectors, adjustable gear, 181/214 cam! Thanks
-
- 6 replies
- 1.6k views
-
-
I have an 02 cummins ext cab short bed 4x4 with an auto. Truck was foggy and lost all power. Had codes P1698 P1689 P0237 which myself and mechanic buddy thought it was a bad vp44. So we replaced it with a new one from thouroughbred. Anyways he put it on and all the codes are still there and nothing has changed. I don't know what to do next!! Also have an airdog raptor and at WOT it still has 8psi
-
- 6 replies
- 1.6k views
-
-
Hello, I have an 01 24v 4x4. I took it on a 200 miles round trip last week. Within 10 miles of the destination I heard a noticeable loud squeal/screech intermediately at around 50 mph. I thought is could be my front pumpkin running low due to a drivers side leak, filled it up and drove home. On way home the noise was still in and out, towards the end it started to become more constant but only above 2-3rd gear. Now when I drive its is constant above 2nd gear at pretty much any speed. It sounds like it could be from the transmission but I was thinking more wheel bearing/ joint. I will jack up rear and update tomorrow. What I have done New driver/passenger side w…
-
-
- 13 replies
- 1.6k views
- 4 followers
-
-
When shifting gears around 2500 to 3000 i can hear an odd noise coming from the passenger side of my truck its doesnt sound like waste gate opening. im not sure how to explain it other than it doesnt sound good, maybe like a squealing type of noise
-
-
- 15 replies
- 1.6k views
-
-
I'm replacing my vp44, removed the old one without aligning the keyway to the 12 oclock position. Is it safe to bar the keyway into position without the vp44 installed? Like my profile says- unskilled (But eager to be instructed)
-
- 6 replies
- 1.6k views
- 2 followers
-
-
Haven't been on the forum for a while, but I think I have a problem & could use some help. I've owned my '99 3500 dually for about 5 years now. When I first got it the lift pump/ wait to start light would energize as soon as the ignition was turned on, but after a few months sometimes (about 50-70% of the time) it would take about 5 or 6 seconds to get the pulse/light. The engine would always crank but it wouldn't light off until the lift pump pulsed. No big deal, just wait for the fuel pressure gauge to pulse then hit the key. Over the years I've read this was an indication of a problem inside the ECM (the computer on the engine block) that requires replacement to co…
-
-
- 5 replies
- 1.6k views
-
-
So i got a 68 ohm resistor and plugged it into the iat plug, cold engine, I let it run 4 min. And nothing but the check engine light came on immediately. Is that normal for the light to come on. Did I do it right and my high idle is not enabled?
-
-
- 7 replies
- 1.6k views
-
-
so I dont have a drip can, i just have a hose hanging down in front of my diff. and I have excessive blow by as far as im concerned for 60,000km.... is something plugged? or done wrong or is there a better set up? i have very high Oil pressure too. 100+ psi cold ( gauge only reads to 100 ) and 50-60 hot idleing. would that have something to do with it? not sure what to build/buy to make this more of a breather then undercoating my truck
-
- 4 replies
- 1.6k views
-
-
Well guys,PureFlow sent me a upgraded replacement for my third failed Raptor 100, and before someone asks yes I did have to pay some extra. For me its worth it as hopefully now I have a reliable truck. The last two raptors died on the road and I had to limp the truck home, and one time it cost me a VP-44. Now I have a newly overhauled VP which runs better than any that I have had before and want to keep it that way. That said, just got the AD ll in and running and cannot believe the difference! The old raptor-100 did fine and held a good 21 psi or so but it did not respond like this one does. That said, PF told me that the pump that I have on the truck now is the same on…
-
- 11 replies
- 1.6k views
-
-
fmi, I was curious to what the mechanical range of the vp44's advance was? I know they are electronically adjusted, but what are the mechanical limitations? Is there anyway to monitor this advance?
-
-
- 7 replies
- 1.6k views
-