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I would recommend the test that Bob Georend described, but use a Digital Multimeter to perform the test instead of a bulb. A bulb requires too much current to illuminate. A multimeter requires virtual
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I don't sell rebuild "kits" for just the OD, but I can get you whatever individual parts you may need.
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Let me know what you need, and I can make sure I have it here. With two large transmission warehouses within 20 minutes of here, I don't keep a very large inventory here at the shop. Do you just want
This is my first post so I'll try to get everything out on the table.
Let me start by saying I have done all of the work on my truck 1998.5 24v dodge 2500. My current mods in my signature are up to date as of today. So first mods into the transmission which is the 47RE included a BD Stage 3 build kit following a goerend triple disk. I drove it that way for a little over 3 months. Money came around now I just recently purchased the ranging pressure valve body from goerend. Still running stock flexplate and shafts(I know not a good thing to do). After installing the new VB everything was fine for all of about 2 days. On the 3rd day is when the problems started.
At this point my truck shifts nice and firm and shifts when it is supposed to. Just no more OD, after I hit 55 lock up engages.. I've gone through and made sure the VB valves weren't stuck. I checked the 3-4 spring and piston no fractures or binding. I have changed my od/lu solenoid and the wiring in the VB for a KNOWN good one. Following that I purchased a new timbos tps as I have had p0222 for a while and after doing moparman's test I found mine was bad. Still no OD. I have not check pressure in the od unit yet... plan to next weekend.
After troubles fixing it my self tried troubleshooting with Bob at goerend, he suggested to run a jumper wire and bulb probe from pin 6 on transmission harness and hook a ground to the cig lighter. He said the bulb should be lit from gears 1-3 and shut off when od is supposed to engage. Tried it. Light never turned on, HOWEVER when I did ground out pin 6 in the cab it made my truck seem to get stuck in low gear or lockup... couldn't tell at 10mph. Waiting for a response from Bob with my findings.
I have gone through and cleaned and test every ground I can find. Running out of forums to scour for new tests. Any advice?