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You have leaking diodes in your alternator. While these mods that you're doing do help the batteries dampen some of that AC noise, you have to fix the source of the noise. I would also put a noise fil
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Soox, I think you need to test the alternator again. It is where the AC noise is generated. The alternator makes AC power. The diode bridge (rectifier) is designed to take that AC wavef
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That's why all the mods get done along with clean body/chassis grounds and good batteries, then test the alternator ac output.
Hello all I am back!
First let me state that I triple checked all of my work. No codes are being thrown at the moment.
Continuing....I just finished the ground wire mod and I am still getting high readings of .062 at idle and nearing .10 with throttle applied (using a Fluke 87-V). Unfortunately, I do not remember my initial readings as the truck has been sitting for a short while but I know they were similar to what I am seeing now. I know of the "second phase" I'd guess you call it with the W-T Mod....new charge wire from aux. battery to alternator (with a fusible link, fuse, circuit breaker, etc.) and adding an extra connection from main battery to aux. battery negative posts. Would I see any change doing that and/or is it high recommenced to even do in the first place?
Where should I go from here? Given that I have not seen any change in readings is the alternator at fault then? Does this line up? I am running the original Denso alternator with new diodes and brushes. I should note, I did accidentally arc my cables once (negative slipped out of my hand when removing it and landed on the positive terminal). Shortly after is when I lost charging abilities to soon find out that my diodes went crispy critters on me.
Kind of bummed out
. Was really hoping to see that reading nice and low. I guess on the bright side I got my rebuilt steering box back from Blue Top and the truck steers a lot better now. Highly recommend!
Thank You all