2nd Generation Dodge 24 Valve Powertrain
This is a discussion forum of the 1998.5 to 2002 2nd Generation Dodge Ram Trucks with 5.9L Cummins 24 Valve Turbo Diesel power train and drive line system. This includes all sub-system including wiring, fuel, oil, exhaust, air, transmission, computers and sensors.
6,288 topics in this forum
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I have an airtex lift pump and it has been great. I changed my fuel filter last night and went to bump the starter and got nothing. My pump in the past has always run after bumping the starter. I got the truck running and the fuel pressure was fine: 18 PSI idle, 14 PSI cruise, never below 12PSI. I have stock fuel lines so it is going to drop a little more than bigger fuel lines. Any thoughts as to why the fuel pump didn't run when I bumped the starter? Would it be some sort of relay issue, computer issue, or just fuel pump issue?
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- 40 replies
- 5.7k views
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I have a 99 Cummins with 109,955 miles on it. I have noticed I had white smoke coming out of the blow by tube but not anything noticeable unless im stopped for a few minutes. if I take the oil cap off it blows a little white out of it but not like clouds of it. So next I did the oil cap test and removed it and flipped it upside down and it didn't bounce around or move (except a little due to vibrations of the engine). the truck runs awesome no lack in power perfect pick up and go, it doesn't smoke except a little black on start up and doesn't eat coolant or oil. No knocking either. The oil pressure is around 30-35 at idle and at normal cruising speeds of 55mph at aro…
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- 21 replies
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Good Morning all, well it seems like every 6 months or so this issue returns, i just slayed that dragon last night and its really getting old. my battery clamps are not going to take much more of this before needing to replace them so here is the low down on the recent findings, the Ground on the primary battery has the acid build up, the other three did not. the problem was only presenting itself at speed between 40 and 50 (in the past, this would happen at any speed above 40mph in OD) i have a switch that i can use to kill my alternator (story for another time) so i killed it thinking it could be related to the alternator and the heat we been having. nope is…
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- 23 replies
- 3.6k views
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I'm getting my truck set up for a winch on a removable mount, that way I can use it in multiple applications. I have a qwadzilla programmer and instructions say disconnect the module before jumping the vehicle, or immediate damage will accrue. My question is, how do you guys use your winches. Or is it only quwadzilla that have that problem. I really don't want to unplug it every time I got to use the winch or even give someone a jump. Unless I'm thinking of this all wrong and it only apply when my truck is dead and someone is giving me a jump.
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- 19 replies
- 3.2k views
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I have a 99 24v 2500 2wd Mostly happens when truck warmed up' It will drop out of OD and sometimes then drop to 2nd. I have dome all the cleaning up etc. I have fresh pink fluid no slipping just wont stay in od mostly. A funny thing is when it does this if you set the cruise it will take off running faster.Trans was rebuilt according to previous owner but don't know who. I have been told that the shifts are controlled by electric in trans. Have not but do intend to replace VSS, but got a feeling it is more then that. Thank you for any help [i do have a new alternator on way for lock/unlock problem.
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- 6 replies
- 1.3k views
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I don't know if anyone is running an enviroguard breather out there, but I just picked one up, and I need to figure out how to get the unused dipstick plug out to install the oil return line. I understand that different plugs were used over the years. Mine appears not to have a lip on it at all, and is just a cylindrical plug pressed in. Any ideas how I should remove it?
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- 4 replies
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I have been experiencing dead pedal some times it is as soon as I take off other times I can drive for 30 min before any bucking happens. I have already replaced the APPS with a new one and it worked fine for about a week or more then it started again. What could be the cause of this to make the sensor keep going out?
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- 9 replies
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Hi Cummins Mopar Fans, Just wanted to give an update on my auto to 6 speed swap. I couldn't be happier. First off, I had everyone on here giving me things to try over the last eight (8) years to help me get my automatic problems solved, gear hunt fix, something like 6 altenators, ground cleaning, let alone hundreds of hours researching trying to find a cure. I want to thank Whie98Lightning for suggesting a swap after he sent me a diagram for the TC lockup switch. Mine even wanted to hunt w the switch on. Like he told me & I agree, that (the switch) was the only thing I could do to keep driving the truck. Also, all the deap pedal issues are gone, the truck seem…
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- 92 replies
- 11.4k views
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What size Tube or pipe do I need for connecting BHAF to the TURBO Boot?? I've been running it for years without one and just soft clamping it over the lip on the BHAF but now i don't think that such a good idea after my latest turbo compressor wheel issues. Compressor wheel was pitted and DAMAGED BY WATER as was told to me by ATS.
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- 8 replies
- 2k views
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Ok, so I bought this truck a few months ago. It was about 4 hours away so I had it shipped home after I went and looked at it. I got a great deal on it. The transmission was completely gone so I ordered a Firepunk Street/Strip trans. It also ended up having a burnt valve which was unexpected. After comparing pricing with machine work and/or just purchasing a new a head I went with a new loaded head from Promaxx. I swapped out the stock valve springs for Hamilton 103lb vavle springs and used ARP Head studs in place of the factory head bolts. Everything is good there. So now after the transmission, head, starter and wheel bearing were all replaced I'm having an issue with …
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- 26 replies
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I had to put OEM filter box back in... mice promptly moved in, trashed filter element. So today I screened the filter with aluminum expander metal & self drill / self tap screws Long ago I used SS pot scrubber behind the hood hinges... where the cowl drains are. Water drains just fine but mice can't get into the heater.
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- 6 replies
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Ok my 2000 nv5600 just died it has a broke gear and what looks to be broken syncro pieces laying in the bottom, the fluid was full and i was not towing i was in traffic at a light and it locked up, now i have a choice to make do i put $3000 in for i 5600 or convert to a nv4500 if i convert i know ill need the trans and bellhousing,flywheel, clutch and drive shafts. My question is will the 4500 bolt in place and will my tc bolt up and where can i find cheep drive shafts they are hard to find here
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- 50 replies
- 7.5k views
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I'm sick of my isolator that goes to my ispro fuel pressure guage. Every so often I get low readings and I have to push back the rubber thingy in the isolator and fill it back up to get it to read right. Would it be safe to eliminate the isolator and have diesel go all the way to the gauge?
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- 14 replies
- 2.5k views
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2000 with Raptor 150, Edge JWA, full 1/2" line from tank to VP, S&B intake. After sitting, she cranks and cranks (5-12 seconds) before starting, and then billows white smoke. I haven't noticed missing coolant so I don't think I'm losing compression via a bad headgasket. Had a bad starter that I replaced and oddly enough a bad vp ground at the same time but this didn't fix the issue. So this leads me to believe I'm losing prime since vp issues typically manifest when hot, not when cold. But my lift pump is tied into a toggle switch on the dash. I can turn on the pump and instantly be at 20 psi right before the vp, so even if I had a small leak, i'd push …
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- 6 replies
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So I'm going to replace X-over tube o-rings and I have conflicting info, Book says torque injectors install tubes torque injector lines, I have read on this forum leave injectors loose (snug but not torqued), install tubes, torque lines, then torque injectors? Is one method better than the other? I understand reasoning, to help center tube on injector. Is the book overly confident that one could put the injector in the proper position the first time? I want to hear from people that have done it. Thanks
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- 17 replies
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ok fellas.. ... i searched for kick down threads and i would think there be alot of threads but no... My main issue is i have to kick the overdrive out to jump out of my lane and pass a car. or getting on an onramp once i pick up speed it shifts to soon unless im really pedal to metal. so when its on the last gear in overdrive there is no going back. I dont like hot rodding all over the place but if i want to pass a little honda its embarassing sometimes.. just put in 100 hp injectors, adjusted bands at trans... replaced intercooler boots.... its got power just not going very far at 1100 rpm... thnx guys for ur help
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- 6 replies
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i have a 1999 cummins with 109,956 on it. The truck starts runs and performs awsome and holds its oil pressures and temp perfect, and it doesn't ever smoke no white blue or black. MY issue is that it has a straight pipe on it and its only 3 inch due to the muffler and cat rotted and removed due to lack of funds to replace them, and now the truck has what sounds like a tick that comes out of the tail pipe. And mostly only when idle. the motor bay is quite with no ticking or knocking anyone have any clue. ps this is my first cummins so i dont know what it should sound like.
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- 7 replies
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While bleeding my rear brakes in the spring I noticed that the back of my muffler had rusted out and the section of pipe going over the axle was dangling by the hangers. I bought a 4" Diamond Eye w/no muffler and a FTE 4"X30" Resonator. I also bought a few preformed band clamps from FTE, I wasn't sure how many I would need, I ordered 8. The old system came out easy, I sprayed the bolts securing the downpipe to the turbo with PB Blaster a couple of times before starting the install. And I had no problem getting them out. The exhaust kit was great, all of the hangers in the kit were correct. The resonator does come with band clamps on each side, I didn't re…
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- 8 replies
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This is my first time reaching out to a forum for help. So please be patient with me. My 2001 Dodge has me stumped. Sorry about being long winded. My truck right now so underpowered it is unusable. 2 years ago noticed a significant loss of power. The truck threw the VP44 code. I bought a remanufactured VP44 from alligator performance in ID & changed out the lift pump. I put on about 100 miles and everything appears normal. I then loaned my tuck to a friend to tow some stuff about 800 miles. During his trip, he received a stellar deal on some fuel from Mexico. From looking at the fuel filters I guessing it was mud mixed with a little diesel. After suspect…
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- 56 replies
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I have to pull my head, and the hoist I had lined up fell through. I can either a new or used 1 ton HF hoist, and am wondering if it will reach our motors. I'm only using it to pull the head, as it's just me, and there are no handy trees around me to help.
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- 12 replies
- 2.5k views
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