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Leaderboard

  1. Tractorman

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Popular Content

Showing content with the highest reputation since 12/09/2024 in all areas

  1. 6 points
    Welp, just ponied up for another year, and I've got to say that this one of the better expenses that I have. The amount of technical knowledge, experience, and willingness to share is outstanding and needs to be supported. For those of you who use this site for information and advise (as I do) remember, it costs money to keep it up and running. Mike and his Mods aren't trying to make money, they're just trying to cover costs. For less than $10 bucks a month we can maintain this site, and continue to have access to one of, if not the best sites for our trucks. Remember, information not shared, is information lost. Mark
  2. On September 6, 2016, I wrote the article "Adding inline power steering filter with system flush" and posted it in 24 valve 2ed generation/Axles, Suspension & Brakes. This is the follow up to that article. Update...7/25/2025 It has been 8years 9months and 44,888 miles since I installed the Magnefine filter and flushed the power steering system, so it was time to flush the power steering fluid and replace the filter again. I used an oil syringe fluid evacuator pump this time to remove and refill the fluid at the power steering pump. The picture below shows the first time the fluid was removed from the system It took 5 remove, refill, and run engine for 4secounds to get the fluid to this clear color, about 2qts. Here is the filter cut open. It looks like the filter could last 60,000+ miles before changing. There was just a fine film on the magnet.
  3. 4 points
    Big thanks to you for getting those computers back to me. Also, I messaged Mike on here this morning and he was a phone call away in no time helping me source this issue! That’s a community This is why I really enjoy this forum. In the beginning we had Dave Fritz/Dodgeram.org, now we have TDR (to some extent). Finally we have this place where all the mysteries have been solved. Don’t forget Mike as we discussed: You may perish of cancer but the forum lives forever, so you live forever!
  4. 4 points
    Thank you for the wonderful comment. Truth yes it's still paying to keep the server alive and keep paying the bills. Remember Mopar1973Man.Com is the LAST PRIVATELY OWNED WEBSITE left. I'm not owned by a corporate clearing house like Cummins Forum which is owned by VerticalScope Inc. Or DieselBombers which is owned by Internet Brands. All these other websites are corporate owned groups.
  5. @Mopar1973Man It looks like he has the updated main shaft already. I purchased several of my transmission parts from Allstate Gear online. The 5th gear nut I used was their "super nut" kit that cane in the master rebuild kit that I bought. I has to replace all 3 shafts, input shaft, counter shaft and the kit came with the full spline updated main shaft as well. My trans was trashed. The main shaft bearing in the front took a massive dump and trashed everything. Also, get a big torque wrench! As Mike mentioned, the 5th gear nut needs to be torqued to 300ft/lbs. DO NOT use a chisel and hammer and think it's good. It isnt. I post some pics of mine below. The carnage More carnage New input shaft and counter shaft New counter shaft in place, reused the small reverse idler. Case has been cleaned here also New main shaft installed, also replaced the tail housing with a cast iron piece. OEM was aluminum and had the mount holes hogged out of round. Now, the shift ring or collar that I have circled in this pic are important! I installed the ring backwards. If you look closely the ring is flat on one side and has a tapper on the other. The flat side has to go toward the large gear to the right as shown in the pic. Due to installing that ring backwards I do not have the use of 1st gear. I don't need it unless towing and I will pill it and make it right, just haven't yet. Hope all this helps!
  6. Well I'm coming back. I'll admit I'm not able to do a lot of jobs. Anything in the heavy lift is over. Currently have Thor stuffed in the house garage and getting ready to go back over the injectors again. Now Thor my 2006 Common rail is my pet project. Like a Phoenix rising from the ashes the new version of me will be going public. Sadly no more wrench time for me. I'll still play with my own rigs. My problem is I've got to consider my stoma and kidneys. So I'll continue my education of the Cummins line. As for my medical issues I'm clean of cancer nearly 6 months. Check up coming. I'm stuck with Stage 3 Cronic Kidney disease this is due to my kidneys being choked by the cancer. The website I'm going to upgrade software and there is a lot of new features coming. Stay tuned in. There is a feature to have live chats again and when the chat ends it will convert the chat unto a forum thread auto-magically. One of many.
  7. Electric Vacuum Pump Conversion: I have deleted my OEM vacuum and power steering pump(s). Instead, I have modified it by replacing it with a midrange setup for steering assist; however, I still need vacuum in order to activate the HVAC controls and to activate my exhaust brake. Although the OEM factory pump never gave me any issues and supplied all the vacuum I needed to work, such as the HVAC and the exhaust brake, the OEM Power Steering did. I have replaced the OEM Power Steering Pump multiple times. In all cases, the pump would not maintain enough pressure and turning the wheels at a stop during idle was almost impossible. Compound that with the inevitable oil leak between both pumps, I figured there was a better system. So, this is where the "midrange" setup comes into play. The 24V ISB was used in multiple applications (not just Dodge). Even though they were not used in another pickup, they were used in midrange sized trucks like Freightliner FL60 &FL80, Ford 650 & 750, Kenworth 370, motor homes, bread trucks, etc, etc. It was the engine of its era. Trucks with vacuum controlled cruise should work also. This particular modification applies to my setup only; (the midrange setup for steering assist). My cruise is ECM controlled. I have the non CAD front axle, so my vacuum demand is limited. On SD applications, they use it to lock the front hubs and HVAC on their trucks. So I feel it should work on any of our vehicles. I used the same pump from the SuperDuty and 3rd Gen RAMS (same pump). I picked it up from Rock Auto along with a Mating Connector. I drilled 3 holes and mounted it on the fuse box cover, in an easy to service spot. For plumbing, it goes to a control manifold for the EB, and tees off into the OEM vacuum line on the firewall. I do not use a reservoir like FORD uses, but you could run one if you desire it. For power, it gets fused voltage from the PDC power stud, which is also the relay supply power (pin 30). The relay trigger is controlled by a fuse tap in one of the PDC fuses, that is hot only when the key is on, so it does not run all the time. The pump has an internal governor, so when it reaches its vacuum threshhold, it shuts off. If it is always running, you most likely have a leak that you need to repair first.
  8. 3 points
    I thought I’d share my recent drivetrain upgrade I put in my 01’ 3500 (SRW converted) 6 spd. On transfer case side of things swapping a NP271D in is pretty common for a 2nd gen. I wanted to take it one step farther. It took some trial & error finding what parts will work and what doesn’t. It’s pretty much a modified Ford design. I found a used 08’ NP271D and rebuilt/modified it. Eliminated the leaky Dodge slip yoke tail housing and utilized the rear fixed flange yoke setup from a 06’ NP273F. I bought the rebuild kit, some updated parts & specific seal installers from TorqueKing4x4. I also installed the Ford style companion flange on my Dana 80 along with a new washer, nut & seal. ***Snap-On # M3586 is the correct thin walled 1-7/8” socket if you ever need it.*** Initially had a 5” aluminum driveshaft but the Sonax slip yoke kit is quite expensive so I had a 4” steel one locally made and upsized it to 1480 greasable ujoints (OEM are 1410). T/case fits perfectly. There’s 1/8” of clearance at the frame and no contact at bottom of cab. The 2nd Gen linkage rod (11”) is a tad short so even set at max travel the shifter will be off just a touch. So I replaced it with the 3rd Gen 16” one and now it’s perfect. I don’t have the cad Dana 60 so the momentary ball switch from the old NP241D-HD just swaps over to make the 4wd light come on. I have the LRG trans crossmember so I didn’t have any interference with the front driveshaft. APPS delete ✅ Midrange power steering ✅ Electric vacuum pump ✅ Next project: Dynatrac high pinion 35 spline Dana 60 3.73 gears with an electric locker… Enjoy!
  9. Mike if you lived closer I would kiss you. I had to remove the t-case boot to replace some wires and left it in neutral. 🤦‍♂️
  10. Transfer case in neutral?
  11. Well the news isn’t good, after talking with the folks at GoECM they have confirmed the processor is bad in my ECM and is not repairable. Thankfully they are applying my repair cost towards the purchase of a new(reman) unit. I would assume this may be why the ACS repair didn’t work. I don’t know enough about these things to know if they would have been able to test this in depth. Their cost was much cheaper than GoECM so I’m not going to say anything negative about them. According to the info ACS sent me it sounds like they tested and repaired the parts I knew weren’t working. I’ll update again when I receive the new ECM and get it installed.
  12. I hope they find what the problem is. Please let us know how it works out with this ECM repair shop so we can update the article "List of Verified and Reliable PCM/ECM Rebuilders" in the 24 Valve 2ed generation engine section.
  13. 3 points
    This is a tech article regarding those who (like me) think the oem spot for the apps is not ideal. Exposed to outside elements, heat, vibration and potential corrosion, moving it inside was most practical. Non Dodge/ midrange applications of Cummins 5.9 24V ISB’s all have their TPS/APPS inside the cab, mounted on the pedal assembly. So nothing is changing on the apps operation, just moving it. This mod does not works on trucks that are auto/use vacuum for cruise. The auto trans kickdown cable is attached to the bellcrank assembly. As with the vacuum solenoid setup too so if you can live without them then it will work. Parts needed: 699-5101 pedal assembly (2x) 6 pin Duetsch connectors kits Zip ties Grommet 6’ of 6 wire harness Tools needed: Duetsch connector terminal pliers Wire strippers Making the mount will be up to you. I can show you pictures on how I made mine but it’s just a one off. Either way you need to mount it inside. First, disconnect the 6 pin Duetsch connector from the apps, remove the bellcrank assembly from the cylinder head. Cut off the cable and discard. The oem pedal assembly will need to be removed and the oem mount has a pivot pin on the bottom that’ll twist out with some channel lock pliers. Once you mount your new pedal to the mount and it’s installed all that is needed is how to control via ecm. So a 6 wire jumper harness is needed. I would HIGHLY recommend removing and tossing the apps that comes supplied with the new pedal and install your current one in its place. I can’t guarantee its quality. If you need an apps, a Williams Control 131973 or 133284 will work perfectly (Timbo is just a repackaged WC). Available from any oem truck dealer (I.e. Kenworth or Freightliner). On your engine side of your harness you need to make a 6 pin male Duetsch connector. Ensure you new connector kits have the locks in them, some kits do not come with them for some reason. YouTube or Google can provide a video on how to use Duetsch connector pliers, they’re super easy to use. Using the hole in firewall that the original pull cable went through install a grommet to prevent rubbing and feed your harness through. If you prefer to drill a hole the same size of the connector body you’ll need a 7/8” drill bit. **It’s easier to make the harness, THEN crimp the new terminals on after feeding it through the oem firewall hole for a cleaner look.** Cut your 6 wire harness to length and crimp on the terminals, install the connector body and plug it in. Theoretically the engine doesn’t know where the apps is so it will work. Make sure you mate up each wire in its proper spot on each connector, if you mess them up a CEL will come on/non functionality of the apps. Secure the harness to various points with zip ties so it’s rigid. This provides a clean look and more room in the engine compartment for future servicing. Start the engine and test. Throttle response should be crisp since there is no cable anymore that has slack as it wore.
  14. 3 points
    Wanted to show something here. Here’s the new APPS, number on it is 133284, same as the Timbo. Even though I ordered a 131973 this is what comes now. You can buy these at any truck dealership. Here’s a pic of my relocation bracket.
  15. 3 points
    I would like to introduce myself to all of you. I met Michael last July in Meridian, Idaho at a medical facility. He had a follow up appointment for his urostomy/ileostomy, while I was getting wound care treatment for my ankle. We briefly met at this place once before but had not been able to chat. On this particular July day, we had a few minutes to chat. As I learned more about Michael's life, I realized that he is an amazingly unique person with a kind heart and good old fashioned values. Upon listening to how he sacrificed on behalf of his mother's need for dialysis in the midst of dealing with his bladder cancer, I began to highly respect and admire this wonderful man. He genuinely cares for people. I knew he was amazingly unique...and I did NOT want to lose track of him. So...I asked for his phone number immediately after he was called in for his appointment. I wanted to know more about him. The crazy thing is that I was adamantly resolved to never get involved with another man at that time! However, we have NOT been apart for more than a few consecutive days since the time we met up at his house shortly after our encounter in Meridian! My interest grew even more when I learned he's a Diesel Mechanic. I was already familiar in auto mechanics, as my dad was an auto mechanic himself doing it as a hobby. I come with a small background in basic auto mechanics...my dad graciously taught me how to do a few maintenance repairs on my own car. To further expand my knowledge base, I have recently joined the Mopar1973man website as Michael's partner, another site administrator and his "soon to be" wife! Our plan is to get married this Spring! We have discussed a few exciting ideas that we would like to implement in the future. We are also working on improving this website for all of you. Be safe out there on those roads!! And...stay tuned!!
  16. WT mod should be done in full first. I don’t have much troubleshooting experience with autos as I have the 6 spd but from what I understand a lot of issues are solved when the mod is done. At least you can rule that out.
  17. We were right, the harness itself was wired incorrectly. IAT and ECT plugs reversed. New harness arrived and problem solved! 3 and 6 both work with correct values displayed.
  18. @mace, I have performed the power steering pump and vacuum pump conversion that you brought to this site. I hope you are still perusing the site and will see this. The time and effort spent on this project (and the APPS relocate) has been very worthwhile. Much engine space has been freed up and the power steering reservoir is right where it should be for easy fluid check / fill. The reservoir is like the brake master cylinder reservoir – you can see the fluid level through the reservoir. An unexpected benefit is that this direct mount power steering pump outperforms any previous power steering pump that has been on this truck. There is no more stopping of the steering wheel when the power steering is under high demand, such as when maneuvering in tight spaces, steering from stop to stop with little forward or backward movement of the truck. I started the project by finding a location for the new power steering reservoir, which was going to be right where the APPS assembly used to be. Then I built a mounting bracket for the reservoir (shown below). The first part of the bracket assembly is designed to let the weight of the oil and reservoir rest in the V slot. In the above photo, note the welded nut where the tab on the top of the reservoir is screwed into the bracket. In the photos below, more brackets are added to fasten the unit to the engine. Below is the new location for the reservoir in the engine compartment - lots of space available for mounting with the removal of the APPS and APPS mounting assembly. I don't have any photos of the actual pump mount, but the mounting is straight forward, especially with the addition of studs instead of bolts. Much easier installation the old vacuum pump / power steering pump combination was. I didn't use a gasket - just the grey Permatex RTV gasket maker. The one thing that Mace did that I should have done (which he clearly mentioned) is to have the pump suction fitting turned down on a lathe from 22 mm to 19 mm to match the 19 mm connection on the reservoir. Because I didn't do that, I have not-so-neat connections from the pump suction to the reservoir (another reason to not take a photo down there). @Mace, thank you again for making this possible. That’s all, folks! John
  19. This is an entirely new method of not just relocating the controller but making one from scratch. It's independent of an ECU. I made a github project with all the details https://github.com/Greatwrk/VP44-EXPLORER
  20. Hey Gang, I've managed to get Thor running for the first time in 2 years. I opted for a stock fuel pump for right now since I'm missing parts yet for the AirDog 150 fuel system I've got I'm looking for a bracket for the pump. I have good positive pressure for the CP3 injection pump. I need to find out what the misfire and studdering are about. Cold start it's a bit long cranking not bad. Once it starts it runs rough and smokes white. I've got a set of @dieselautopower +50 HP injectors installed and had them sent back to DAP and found one injector had an issue and was repaired and sent back. Then I ordered a set of o-rings and replaced all o-rings on injectors and cross-over tubes. Once warmed up all roughness is gone. It runs good and strong for what it is. I can even do the oil cap test and the cap does not even move. I'm trying to figure out the cold idle roughness and warm up smoke them once warm it drives and runs great. Even yesterday I drove to town and got 50 dollars of fresh diesel fuel to make sure its got enough cetane and pour point depressants. Currently 39*F here. Last problem in this category is the grid heater light came on yesterday and dinged 10 times signaling its high flow rates of the CP3. It idles at about 7,9xx PSI of fuel rail. At 1,500 RPM its pumping up to 11,8xx roughly and appears the fuel rail is building good pressure. With Thor being my project I plan on writing articles as I get things figured out. So anyone give me a hand on this? Monday I'm going to put insurance and registration on Thor and he's going to become my daily runner. Why? Beast finally needs shop time and the rear main seal is leaking. Thor becomes the primary rig for now while I gather supplies for Beast and get my help here to remove the transmission and transfer case so we can access the rear main seal. Thor is also going to lose the heavy flat bed and front bumper soon. I'm going back to the lighter factory box and tailgate then factory bumpers and ditch close to a full ton of steel. Thor is fat at 9,300 pounds even empty.
  21. Glade to hear it. This means that GoECM fixed what ACS could not. A big plus for GoECM.
  22. as always, I get freaked out if my truck is "down" and opted for the fastest (most reliable) fix. This is why I try to be proactive about maintenance instead of reactive.
  23. After some thinking and talking to the wife, I’ve decided to send the ecm to someone else. I think the problem with ACS may be that their repair is based solely on the information I give them. The shop that fixed my turbos recommended a place they use out of Texas. I called them today and they test and check the entire unit. Just found out today my daughter can’t take drivers ed for a few more months so I’m gonna use the money we saved for that to get it done.
  24. Sadly I have nothing to "work" it with... it is back to daily driver status... I may hook onto the trailer and go pickup some firewood but even that isn't "working" it like I KNOW the truck likes. :) and the NOT WET status inside and down stream from the turbo is what most perplexed me... I was expecting "wet" as well.
  25. Heater hose will work for the drain to block connection.
  26. Just remember just one wire pinched in behind part, bolt, or bracket could do it. I had one where the PCM burned up because one wire was rubbing on the trans dipstick tube and fried the voltage regulator.
  27. I ordered a front drive shaft from Torque King today. The sell strap and bolt kits for this application. https://torqueking.com/product/40709/qu40709-universal-joint-strap-and-bolt-kit-for-spicer-1350-or-1410-yokes/?searchid=1393311&search_query=driveshaft+strap+and+bolt+kit
  28. I appreciate the phone call as well. Good to chat with someone that actually knows what they're talking about! I hope to update this next week with a solution! This has been an ongoing thing for years now!
  29. This photo is of a typical 12 valve engine. No crossover tubes. Fuel line are connected directly to the injectors, so injectors can be shimmed. John
  30. I'll see if I can get a picture of mine during lunch.
  31. 2 points
    You guys!...., that piston is not in backwards - that cylinder is only supposed to be used when backing up! - John
  32. 2 points
    Congratulations
  33. 2 points
    Currently I have a wif sensor in the airdog water separator. Removed the drain and put the sensor in. I ran a jumper harness from that to the engine harness plug. Like I mentioned I unplugged it at the harness side and it’s still stays on. I’m not sure if this is a problem from ACS. I did order a new apps through my work (Inland Kenworth). Williams Control 131973. I should have it by Tuesday. Hopefully it solves my P0122 issue, I will check the wiring harness I made when I relocated in on Monday to confirm is not melted or something.
  34. It is possible. I have worked on a few common rail Dodge Cummins engines. What I have found is that it can be very difficult to troubleshoot this fuel system, even with the use of the right diagnostic equipment. You may be fairly certain that a high fuel return rate is occurring, but that could be caused by a leaking PRV, a CP3 pump, one or more injectors, crossover tube / tubes not seating, etc, or even a combination of the these. It is for the above reasons that I would want to prove (which can easily be done) that there are no issues with fuel supply, first - then move on to other diagnostics if the fuel supply is good. One thing for sure..., if there is a problem with the fuel supply, then the high pressure part of the injection system cannot run right. - John
  35. Sorry for the late update. I was able to replace 5th gear and make it home without issue. It was a heck of a lot harder to torque that nut to spec than expected, but I got it and it seems to be holding fine for now. Thank you everyone for your help!
  36. Not a problem and your welcome always here to support the Cummins family.
  37. Give Module masters a call in Moscow Idaho. https://mopar1973man.com/vendor.htm/vendor/module-master-r8/
  38. I had a feeling that you would go back to the first running board after you had better results with the second running board. That's not "OCD" - that's a "good decision"! - John
  39. 2 points
    I'm alive and cancer free yet. I go in on Jan 28 for testing make sure my cancer doesn't return.
  40. Armature shaft binding when cold. See if tapping on the housing frees it up.
  41. The winter covers definitely work. I bought mine from Genos 2 years ago. What a difference in the winter. Warm up times are much shorter and she holds heat a little better also.
  42. I went for it yesterday on the first running board top skin. Those long beads are tough to try and keep straight. Did I? Mostly.....at least its gonna be Rino Lined and not gloss back!
  43. Have you ever considered an Alice Cooper look? Mark
  44. All your testing are no good. You need a DVM capable of less than 2 volts AC with multiple frequencies, not just 60 hz. A household DVM will do this, which is why your test data is confusing. Look for a DVM like a Fluke or SnapOn DVMs which are very capable of multifrequencies and voltages less than 2 volts. Just look your DVM has a 200 VAC setting too large. Needs to be 2 VAC or less.
  45. Hey Mike, I contacted Quadzilla Monday and they are sending me out a new PCB board and switch. I will keep you updated on how that turns out. They will send me a wiring harness if that doesn't correct things.
  46. Yes sir you can. Just key on and click the switch through the different modes and report back the values seen.
  47. Yup. Im still here plugging along slowly but still going forward.
  48. We have pumps on the shelf. We also have seals. If that is a an option/ you can determine the part # you need. There is an exploded view picture and part #s here http://www.sparesbosch.ru/results_bosch.php?article=0460426114
  49. Sadly. I would remove the injection pump and see about getting a rebuild kit and replace all the seals including the front seal too so the diesel fuel doesn't leak in the crankcase. Reman pumps are available from @dieselautopower . I would consider that being the governor spring and other internal parts do wear out. So before performing any repairs I would highly suggest removing the pump from the truck. That cover should have 4 Allen bolts holding it on. Be careful the Governor Spring is attached to the cover and could be replaced but be careful not to stretch the spring. Serioyusly I would just consider a reman'd pump at least then the pump is in good shape to keep running.
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