2nd Generation Dodge 24 Valve Powertrain
This is a discussion forum of the 1998.5 to 2002 2nd Generation Dodge Ram Trucks with 5.9L Cummins 24 Valve Turbo Diesel power train and drive line system. This includes all sub-system including wiring, fuel, oil, exhaust, air, transmission, computers and sensors.
6,286 topics in this forum
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I haven't had my truck long only done a few upgrades. Got a few questions I have been slowly replacing my vacuum lines after finding them with holes. My question is why does sometime I have more blowby then others and yes its warmed up sometimes it's nothing coming out vent tube and sometimes it steaming pretty decent. I did the cap upside down test and it doesn't move and it doesn't tea kettle. What would cause this? Next question is I changed my oil with 15w 40 delo 400 after driving 1000 miles the oil is still clean and clear I'm use to diesel oil being black soon as u crank it and check it. Is this ok or something wrong? Last question is I had a intercooler boot cut I…
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- 18 replies
- 2.9k views
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A week ago my wait to start light would flash when i turned the key on but would not power the grid heaters. I replaced the relays and the IAT. Now the truck is throwing codes P0382 P0380 P0237 P0341 P0113. I know what the codes mean but I was hoping someone had experienced this and could help with the diagnosis. Truck is running rough intermittently, at idle it is pretty rough and when driving it is hit and miss. I started the truck about an hour later and now the check engine light isn't on but it is still running rough. All help is appreciated. Thanks.
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- 8 replies
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My 01 started running a little rough intermittently. It did it once and quit. Hell I thought it was a glitch but about 3 weeks later it was running rough again. I changed the fuel filter with no change. Then I changed the lift pump and it ran better but not good. I wasn’t having any issues with it starting at all, just randomly would get loss of power. At this point I was still driving it to work but it was getting worse. You could turn of the key going down the highway and boom it would run good again, maybe for a minute or the rest of the day. It finally got to where it would take a few minutes to start so I went ahead and changed the VP44. It ran perfect for 2 days and…
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- 4 replies
- 2.8k views
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Does the plastic radiator drain plug only turn 1/4 turn to open? Or does it screw all the way out? My fluid looks clean ad green but 1/4 turn it doesnt drain..... I tried blowing air into it to clear anything . no luck. Does it screw all the way out or just 1/4 turn... Dont want to break it... Dont remember this issue last time I replaced my coolent any tips PS does it turn 1/4 turn then you pull it straight back / out? Thanks
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- 20 replies
- 3.3k views
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A little background on the truck. I have owned it for about a year and the first thing was dead peddle issues, it wasn’t bad just some hesitation sometimes then the crank sensor went out so I replaced it and eventually put a Timbo apps in it. It has always thrown the P0222 since replacing the TPS but ran fine. I developed a bad oil leak around the vacuum pump. I removed the bolt holding the wiring harness to the side of the block to pull the wiring back for better access to the pump and have been getting the following codes ever since. My tach will go dead all other gauges are fine and the truck will lose power but not die. Usually after I drive it for about 20 minutes it…
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- 5 replies
- 2k views
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Installing a new deep oil pan and filter decided to replace all the solenoid and the 3/4 spring. I want to install the new overdrive and tcc solenoid without removing the valve body. Can this be done if I just remove the zip ties and reuse the original harness? Or am I missing something?
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- 3 replies
- 8.6k views
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Yup, Friday the 13th and a full moon has struck me... Got the transmission and clutch done went out for a short test drive and came back check for leaks or issues. Sure enough the driver side tank blew out started leaking just above the drain cock. Redneck fix. I cut the vacuum breaker off the radiator cap. This will allow the pressure to escape the radiator and not build pressure. I made 84 mile test drive and no issues. I've got a replace radiator in Ontario, OR waiting for me. $282 dollars for a replacement radiator. Oh well... Radiator lasted 392k miles and header tank seal failed.
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- 29 replies
- 4.6k views
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Been noticing mist or smoke in the headlights. Yes I yanked the bottle off long ago. Hoping valve seals is all. It doesnt use any coolant still runs the same also doesnt use oil. I am 1/4" over the hash mark on the dipstick but I doubt that's it. But who knows. Odometer reads 323k not sure I trust it. Never had more than a valve adjust. Is it time to upgrade the head? Hoping its semi normal and I'm just noticing since about 90% of my driving is in the dark right now. This is first year in about 8 that I've used her for work.
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- 12 replies
- 2.3k views
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I installed a Fass Fuel pump & water seperation system & in the instructions it simply says unplug the power for the stock lift pump. Well needless to say that equals codes & Fass tech support had 2 suggestions. 1. leave it uplugged & if the code bothers you some code readers will erase that code from the system. Umm no. 2. If you go to an auto parts store you can by a resistor, "I believe it's 5 ohm & plug the power line into that & it simply tricks the ECM into thinking that it is plugged in and working fine. (hmm sounds like a guess, guessing I can do on my own thx) So anybody have a better idea? I'm actually getting…
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- 9 replies
- 1.8k views
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I rebuilt my 47re all new parts with a ATS rebuilt shift solenoid. On cold start shifts fine until you you stop it doesn’t down shift and it then starts in second gear and will not go to over drive. basically have reverse, second and drive. (scanner indicates short in solenoid)
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- 4 replies
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Between selling stuff and saving, I have some extra fun money to spend on making my truck more powerful and hopefully more efficient. I see that DAP has Adrenaline units on sale, so am about to bite the bullet on one of those. I do have some questions as to what other items should be on the shopping list. Here is a list of what I do have or will have done in the next couple of weeks: EGT gauge Fuel Pressure Gauge Modest lift pump (FASS DRP relocated to beside tank with Draw Straw) 3" Exhaust Automatic transmission in good shape, but so far as I know it's mostly stock (accumulator piston, governor pressure solenoid, Servo Cove plate, pres…
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- 7 replies
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I have a 2002 dodge 3500 24 valve Cummins 5 speed manual, got in it the other day to move it and it fires right up but noticed when I put it into first gear I have no throttle but idle, could this be a apps faulty ?
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- 11 replies
- 1.4k views
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Was having over boost issues and when I put air to my wastegate it wouldn’t budge so I pulled the turbo thinking the valve in the turbo was froze. Got it all apart and turbo is nice and free but I noticed that the actuator rod was stretched out pretty good. Does this look normal? Or did the fella crank the waste gate down to get more boost
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- 8 replies
- 1.9k views
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Having a strange issue that I'm trying to figure out and hoping one of you guys can help out? Just joined here but been a member of the other place for years. Anyway I've got the 2001 mentioned in my signature and I'm getting ready to take a 1200 mile trip on Friday, but having an issue with my truck that just started last week? Basically I randomly experience a total power loss, but the engine doesn't die. More like total loss off fuel or throttle control. Fuel PSI has never been an issue and is the real reason I bought the iQuad. Pump is tapped but rarely use it as I'm really just trying to run stock. I've been running with "0" level for the past few months and t…
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- 10 replies
- 1.7k views
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1999 dodge 2500 Auto new batteries Grid heater deleted Everything else pretty much stock I replaced my alternator in preparation for getting my ECM rebuild. Installed my rebuilt alternator after they replaced the brushes, diodes and rectifier. Started the truck. No charge. Alternator got very hot. Went and got a brand new alternator.. Same thing.. I am looking for help!! Where to start trouble shooting. Hoping the PCM isn't fried too! I am headed to the store tomorrow to buy a new multimeter, mine broke recently, to check the green wire coming off the alternator. Im more worried there is a short somewhere in …
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- 21 replies
- 10.4k views
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Hi everyone my name is Andrew and I'm brand new to the forum. I was hoping you could help me with my ECM problem. I have no idea what caused my ECM to fail.. Is this a common issue? Do I just replace it and cross my fingers or do I need to investigate further? The truck ran just fine until I pulled in my driveway (luckily) and it died. I had it checked out and was told the microprocessor fried and the ECM is deemed unrepairable.. Since I can't buy a new one (discontinued) do I buy a used one with no warrantee or do I get a reman unit? If reman who do you recommend? I've called a handful of remans companies and every place seems very shad…
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- 46 replies
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Anyone know what this thread size is and what its actually called? 1/8" ntp screws into it but this is a straight thread that seals with an o ring. NPT is tapered. Thread pitch gauges are at the shop
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- 7 replies
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So long story short truck has a nv4500 swap from an 01 with an 02 motor that had the auto. Truck is extremely gutless until around 2000 rpms. Once you hit that it’s a completely different truck. Has an air dog that keeps 18psi fuel pressure. Have cleaned both iat and map. Can free rev all day but once you put a load in it there is a very noticeable lack of power. Checked codes and only codes I am getting are for the auto trans.
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- 24 replies
- 3.1k views
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